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8 <br /> <br />Per the RCWD CAPROC dated April 8, 2020: <br />Soil conditions vary over the sloping site, with HSG D sandy lean clays (CL) at the higher <br />elevations, and HSG A/B poorly graded sands and sands with silt (SP/SP-SM) with sandy lean <br />clays below. The HSG D soils in addition to the high water table below the HSG A/B soils <br />make infiltration infeasible for the site. Thus, stormwater ponds are acceptable to meet the <br />water quality requirement. The pond sizing, and outlets and overflows are consistent with <br />design criteria. 100% of the project area either flows to the ponds or meets design criteria. <br />Additional TSS removal is not required. The applicant has met all the Water Quality <br />requirements and the design criteria of RCWD Rule C: Stormwater Management Plans. <br /> <br />Discharge Rate Comparison <br /> 2-year (cfs) 10-year (cfs) 100-year (cfs) <br />Existing Proposed Existing Proposed Existing Proposed <br />North to Private Ditch 3.5 2.3 5.1 3.9 6.9 5.7 <br />West to Private Ditch 11.6 9.2 6.8 34.1 28.7 25.7 82.8 74.7 73.9 <br />South through <br />Culvert under Birch <br />Street <br />4.4 3.5 8.0 6.5 14.6 11.9 <br />Totals* 19.2 12.5 9.8 46.7 35.6 32.2 103.3 87.8 87.0 <br />*Difference due to time of concentration <br /> <br />Post-development stormwater discharge rates are less than the pre-development rates. <br /> <br />The City’s stormwater management requirements for rate control and infiltration have also <br />been met. The City’s requirements for rate control and infiltration are the same as RCWD. <br /> <br />The applicant has submitted the revised plans to RCWD for final review and approval. RCWD <br />approved and issued Permit 20-002 on July 20, 2020. <br /> <br />During the Public Hearing for the project, there were concerns raised by a few of the adjacent <br />property owners. Staff, the developer, and developer’s engineer have worked to address these <br />questions. As a result, the downstream ditch conditions were surveyed to obtain baseline data <br />of the existing conditions. A culvert on the Rehbein parcel was reviewed by the property <br />owner for blockage. The proposed outlet and associated drainage and utility easement to the <br />Vickers’s parcel is being processed. <br /> <br />The original design for Pond 100 outlet was a conventional outlet structure and discharge pipe. <br />This design required a drainage and utility easement. Note there is an existing Great River <br />Energy easement that already encumbers this same area. The Vickers were concerned about <br />the proposed outlet discharge and thus granting an easement was declined originally. The <br />developer then re-designed the outlet without an easement. This revision included a plunge <br />pool dissipator and enlargement of the pond. However there were still concerns regarding <br />erosion and overland flow. Staff met with the Vickers on Thursday, May 7, 2020 to review <br />options for a stormwater outlet. The owners explained their concerns over possible ditch <br />erosion and ongoing maintenance concerns. Staff explained that if an easement is obtained, the <br />City will be responsible for ongoing maintenance of the improvements including the outlet <br />area. The owner informed staff of their preference for a piped outlet with a dissipater still